ok guys im not sure whats going on here. i thought the carb base gaskets were leaking so like any good person i changed them $6.50 no big deal. Now i was on lunch break at work(i work for the local honda car dealer no haters please) they have a parts cleaner there. If u work at a dealer u know what i mean. i did not and i repeat this did not take the carb apart. i didnt have a rebuild kit for it. Before i did this the bottem gasket was wet looked like gas not oil, and it was holding and loading. could smell alot of gas almost to the flood stage. Now it will flood itself out without hitting the gas if it turns long enough. I know what your thinking choked isnt set right. Well sorry guys already ahead of the game. the auto choke is set right the manual one u all think it should have has been replaced already. tonight on my way home from work it was running good no lagging or anything like that. let it sit 2 hours and left again and OMG its worse that it was when i started its like im
not sure what to do here. they way it is i may have to do a full top end on a motor that was just rebuild for a mudder truck. guy said that sold the motor didnt have enough power for him went to a 427 i think or 460. i just dont know what to do here i have an exploder that runs when it wants too i mean litteral and i got the truck as a project/everyday driver kinda deal. cant have them both not running right and cant afford to do a top end on a motor ether. Suggestion anyone any help is nice.
thanks guys.
jeremy

thanks guys.
jeremy